- Joined
- Jul 12, 2010
- Messages
- 5,618
- Reaction score
- 3,981
- Location
- Killingworth, CT
- My Car
- 71 Mach 1
71 XR-7 hardtop
71 Country Squire
65 hardtop
72 Country Sedan
69 XL sportsroof
Just for giggles, since I'm home bound for at least another week +, I pulled down the 351C-4V out of my dearly departed 71 XR-7 4 speed car.
I bought the car out of NJ for the paltry sum of $500 back in 2003. A true M-code 4 speed XR-7, still running, but had a fairly loud knock. The guy I got it from bought it from a used car dealer in PA. Anyway, I did a quick thrash, replacing the bad shortblock with two spun mains, with one from a great running but wrecked 72 351-2V Cougar convertible that I parted out, so it still had the flat tops. I swapped the 4V top end, Comp 280H cam and lifters over, did valve seals and gaskets and had it running in a couple days. Gave the OE Autolite 4300 my best college try and after a couple weeks of no progress and 8mpg, pitched it on the shelf and ran a Holley 800DP with a thick spacer gasket. Thing ran damn good and other than the noisy fricking Crane Hi-Intensity lifters, it was a hoot to drive. I did a Duraspark swap, tossed the factory flex fan for a clutch setup and would consistently pull down 16~18 mpg. Fast forward to 2006, I got rear ended not 300ft from my house and totalled the car. She was a bit rusty, so the impact did a lot of damage. I did get a good insurance payout, but after getting screwed on a supposedly rust free car on eBay, I decided it was time and parted/liquidated all my Cougars.
So, the engine's been sitting under my bench since then and with the "free" time on my hands, I figured I would do something with it. Did a quick degrease, wire wheel cleaning and blow off to make it a bit less disgusting and proceeded to take it apart.
Ewwwww....
Everything looked as expected until I pulled the intake and found one bent pushrod on #6. At that time, it reminded me that there had been at least one bent pushrod when I tore the original engine down.
one of these is not like the other....
Apparently it had been like that for a while.
#1 intake and #5 exhaust lobes weren't giving full lift, neither was #4 intake.
Like I said, this was a car that I drove daily and it was running great up to the accident. Pretty much every lifter was showing signs of failure.
I bought the car out of NJ for the paltry sum of $500 back in 2003. A true M-code 4 speed XR-7, still running, but had a fairly loud knock. The guy I got it from bought it from a used car dealer in PA. Anyway, I did a quick thrash, replacing the bad shortblock with two spun mains, with one from a great running but wrecked 72 351-2V Cougar convertible that I parted out, so it still had the flat tops. I swapped the 4V top end, Comp 280H cam and lifters over, did valve seals and gaskets and had it running in a couple days. Gave the OE Autolite 4300 my best college try and after a couple weeks of no progress and 8mpg, pitched it on the shelf and ran a Holley 800DP with a thick spacer gasket. Thing ran damn good and other than the noisy fricking Crane Hi-Intensity lifters, it was a hoot to drive. I did a Duraspark swap, tossed the factory flex fan for a clutch setup and would consistently pull down 16~18 mpg. Fast forward to 2006, I got rear ended not 300ft from my house and totalled the car. She was a bit rusty, so the impact did a lot of damage. I did get a good insurance payout, but after getting screwed on a supposedly rust free car on eBay, I decided it was time and parted/liquidated all my Cougars.
So, the engine's been sitting under my bench since then and with the "free" time on my hands, I figured I would do something with it. Did a quick degrease, wire wheel cleaning and blow off to make it a bit less disgusting and proceeded to take it apart.

Ewwwww....

Everything looked as expected until I pulled the intake and found one bent pushrod on #6. At that time, it reminded me that there had been at least one bent pushrod when I tore the original engine down.

one of these is not like the other....

Apparently it had been like that for a while.

#1 intake and #5 exhaust lobes weren't giving full lift, neither was #4 intake.


Like I said, this was a car that I drove daily and it was running great up to the accident. Pretty much every lifter was showing signs of failure.
