Been very busy on many fronts lately and realised I did not post an update for a while now. So here's a glimpse of what i've been doing...
On the mustangs side of things, it's been heaven for a few weeks. The weather was terrible most of the weekends but the moment it was dry, I could enjoy taking the 73 for a spin into the nice surroundings of my town. Put a few hundred miles on it..
Back home or forced to stay because of the rain, I've been busy on the 71. Done lots of time consuming things, here for instance, I've started to look at the gearbox
Removed the pitman arm, and because the one I got was delivered with a cheapo finish, basically oil on raw metal, plated it, and while at it all the bolts and nuts of the unit.
Because this unit is out of the car only once every 50 years, it doesn't leak and has no play, but I have ordered a rebuild kit that should arrive in ???
That's a big question mark, as after placing 2 orders at NPD and not receiving/hear anything while I'm used to a good service from them, I've contacted them and a manager there told me the entire sales team is home with covid and the team supposed to replace them contracted that shite as well!
Short story, that rebuild kit and many other parts I need badly are waiting for NPD's immune system to kick in...
Bad news or not, stuffs needs to be done, so continued to restore other badly corroded dirty parts like this coil spring, now looking bits better than it used to!
While making bubbles, I've also been busy repairing the last damaged apron, it now regained the strength you expect from it and is not longer having that swiss cheese look I hated so much!
Making the patch took a while as folding it to match the exact shape was more easy said than done.
Also removed, derusted, plated and welded back the reinforcement for the bolts.
I still have one patch to go on this apron, just under the cowl vent and fire wall, that was butchered at some point to reroute the lights harness under the fenders. Because the cabine metal has also been butchered (now fixed) where it connects, and because my garage is too small to even think about having a loose dashboard around, I will make some temp patch till I can safely weld it without the risk of fire as there is plenty flammable stuff behind the firewall. I'll post on that once I get to it.
I said above it was heaven. Yeah driving and restoring at the same time been a blast till last saturday! For once not only it was dry, it was also not so cold and sunny, so took the lady green for a ride. After +- 50kms enjoying the dutch mountains, I went back home and while I was at a stop light after a not that legal run, I noticed smoke on the other side of the car...
Lucky me, I was just a mile away from my house. So inspected and discovered that my rear end started to leak onto my brakes... niiiiice!!
So ordered parts to fix that, as the axle needs come out, new shoes, bearings, retaining ring, gaskets etc... Lots of fun awaiting ahead for me!!
But there will be no fun till NPD sends me my parts!
Oh well, there is another and last thing that is leaking on my 73: the FMX. I had that plan to swap it with an AOD for a while, but when I was underneath checking the rear end leak, I've noticed that the leak has become worse.
So as the car will not drive any time soon again, I have started to work on that AOD swap that I want to do for years. It's not the one from my 93 T-bird as my friend prefers to keep the car movable (gave it to him).
Instead got another one he had laying around, a 87. As I will restore it completely, I don't really care if it was ok, low or high mileage or perfect. The trans will be as new when I'll mount it under the 73.
Already took contact with Ken at bad shoe and I'll be learning the guts of that baby coming days to be able to inspect it and order what I need this next weekend..
As you can see on the previous pict, the casing was seriously corroded and filthy (not leaking tho). So before I even think about opening it, I needed first to give it a massage, first with high pressure, brushes solvant and TONS of elbow oil!
It took a while, in fact most of the afternoon, but ended up with a much cleaner unit. I even tooks some time to shave many casting flaws, not just to please my eyes, but because most were sharp and I was tired look at bleeding finger tips!
From one blur to the other, ended up filing loads!
Like my 71 C6 that I did last year, it will be painted and just need be clean/oxide free for a nice long lasting result.
Yesterday it was time to start remove a few things, not planning to empty it without knowing more, but removing the pan/draining it, remove the body and take some picts should be safe. Also removing the front pump should be easy and quickly done...
NOT !!
Turns out the pump did not want get out. Once the bolts are out, only the o-ring keeps it in. It should come out easy after a good pull they say... well they lied!!!
After a long time looking at a way, having some kinds of metal constructions in my head to build some kind of extractor, I saw that on 2 of the pump casing's holes, there were threads.
Not the bolts thread but bigger. And then I got it. Pretty sure Ford had these threads set into the pump casting for a reason! THAT REASON!
And here comes the tip for those having the same issue: with a rubber mallet, wood, whatever, after you have the o-ring full of penetrating oil, tap from the side to rotate the pump just enough so the trans casing holes no longer align to it. Insert bolts (ones with that thread less tip) and screw gently till the tip reaches the body and starts to move the pump outward.
Of course if you are in Europe, because the expected bolts are not metric (while the other bolts on the trans are or seam to be) it will cost you some time to find bolts that would fit (trust me it did!), that would be long enough and strong enough (you don't want to break one in there so make sure its high grade). Lucky me, I never throw away any US used bolts and have a box full of them, collected over the years. The only ones I had that would fit were just a tad too short but with a strong grade. All clean and oiled, I took my time and went slowly applying torque, till they were at their max length so finished by pulling while hammering and after 3 hours (yes it took me 3 freaking hours to get that pump loose!!!), I could enjoy the sight of what was beyond it...
As you can see, I had a quite busy mustang life in these past weeks
The 73 as now the prio to return on the road asap, but as usual, i will continue to work on the 71. Even if that is only one little thing at a time, progresses will and are made each and every weekend on it!
To be continued...