- Joined
- Sep 12, 2015
- Messages
- 7,892
- Reaction score
- 3,006
- Location
- SW Ontario
- My Car
- 1971 Mustang Mach 1, M code, 4 speed.
Over the past while, I guess I've been a victim of fear. False Evidence Appearing Real. My engine was using oil more than what I would consider normal, Loads of spark rattle, suspected burned pistons etc. etc. Many have commented on this issue. I was afraid I would loose my numbers matching ( yes it DOES have the VIN on it) block, but today I got some good news for a change. The engine has been stripped and thankfully the bores are all good. It will just need freshening up and new pistons and rings to lower the compression ratio to a more manageable 10:1. Recalculating after measurements showed I was right about it being way too high at 11:1 for 91 octane Shell, best I can get here without ethanol. What we did find that has us a bit baffled is the cam has wear on some lobes and lifters, but not on others. It was a Melling MTF-2. It has always been run with zinc additive and good 10W30 oil. My engine shop is going to have it tested in case it is a bad cam from the factory, wouldn't be the first time! This engine only has 5k miles on it. The next issue to address is the reman. factory distributor, which will be recurved and likely put back to points, for now anyway. Also, we will be looking more closely at the carburetor which is a Holley 670 Street Avenger. It seems to run well on it, but I think a trip to the dyno will be in order for fuel /air ratio checking. Looked good the last time the car was on that dyno, so I'm not expecting any issues there.
I'll post more later as I get closer to actually running the motor in car.
Geoff.
I'll post more later as I get closer to actually running the motor in car.
Geoff.
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