PeteG41
Well-known member
- Joined
- May 18, 2022
- Messages
- 353
- Reaction score
- 205
- Location
- Tempe, AZ
- My Car
- 351c 2v, FMX Transmission. Ordered from Sanderson Ford in Phoenix, 99k original miles.
Hey guys, just some questions for the experts. Finally got my dream car about a month or so now and getting some things done. Just rebuilt the carb, and after doing so found out the fuel pump was shot. So spent the morning yesterday replacing that. Jeez they don’t make that top bolt easy to get to.
Changed the oil while I was at it since the filter seemed partly in my way. Whatever gunk was around the drain plug was hiding the fact it’s stripped, so now I’m getting a slow leak out of there. What’s the easier fix for that? The idle is a little bit all over the place, but completely smoothes out at 2k rpm’s. Then it will go from about 1k, drop to 650-700 like it’s going to die, and then the rpm’s bounce back up. I was told this motor was rebuilt back in 2015 or so, but something seems off. 99k original mile but has been sitting for a bit. I’m checking the timing tomorrow and hopefully that solves a lot of it, but I’m not too optimistic unfortunately. I thought about running a can of Berrymans down it so try and wake up the top end, maybe a stuck valve or something. I’ve recently been getting a decent amount of smoke, assumed it was just burning carbon buildup from some shots of carb cleaner spray. Any input is greatly appreciated.
Changed the oil while I was at it since the filter seemed partly in my way. Whatever gunk was around the drain plug was hiding the fact it’s stripped, so now I’m getting a slow leak out of there. What’s the easier fix for that? The idle is a little bit all over the place, but completely smoothes out at 2k rpm’s. Then it will go from about 1k, drop to 650-700 like it’s going to die, and then the rpm’s bounce back up. I was told this motor was rebuilt back in 2015 or so, but something seems off. 99k original mile but has been sitting for a bit. I’m checking the timing tomorrow and hopefully that solves a lot of it, but I’m not too optimistic unfortunately. I thought about running a can of Berrymans down it so try and wake up the top end, maybe a stuck valve or something. I’ve recently been getting a decent amount of smoke, assumed it was just burning carbon buildup from some shots of carb cleaner spray. Any input is greatly appreciated.
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