Mike Bunch
New member
- Joined
- Feb 15, 2016
- Messages
- 4
- Reaction score
- 0
- Location
- USA
- My Car
- 1971 Prostock Nostalgia Dragster
I purchased a never completed 1971 prostock race car roller that had not been touched since 1970. Its a real ford body in white and appears to be a factory sponsored car.
I found the paperwork for motor work done from Paul Machine in Jupiter Florida from 1970 and tracked down the man who owned the shop who is known on 7173 as Paul of mo and he still had the motor so I was able to buy a vintage boss 351 prostock that was built with all of the best tricks and mods of the days. I have talked more to Mr. Paul in the last few weeks. He did not sell the engine because rules changed and Ford droped out of draagracing in 72. He said the engine was an experiment and he couldn’t sell it. Heres why.
The crank is stroked for 6 of the 8 rods. In the car the tech inspection could really only check the front 2 sparkplug holes for the stroke. The more cubic inches the motor had the bigger the weight penalties.
The distributer is a one of a kind homemade part that does not work like anyother dist and it does not have a limit to how fast it can work.
The heads have port plates and intake side stuffers with titanium valves and springs. The block is all rerouted for the oil and has lines running everywhere. It also has been set up for a vacume pump system to take the pressure out of the engine for more hp.
It has a homemade tunnel ram that was made to fake a weiand but works above 10000rpm.
New stuff,
We discovered that the bottom of the intake that covers the valley had 2 parts and was hollow inside with a passage cast into it that runs up to a intake bolt hole?? We found another port inside that had a tiny pressure valve in it but did not go anywhere?? I called Mr. Paul and this is what he told me.
1 of the intake studs was hollow and had a hole in it that lined up with the hole in the intake. You could screw a line onto the top of the bolt and pump nitrous into the manifold. The other valve could be shimmed to open at about 450 pounds. You filled the intake to about 400 pounds when the motor was cold. When the temp went up then the pressure in the chamber went up with it and once it hit 550 it would open the valve and let the gas flow threw very small wire drilled passages that runs to each intake port. It took about 2 min for the gas to go out. That would be long enough to do a burn out get set up and make a pass before there was no more gas left. The holes are so tiny that you can not even see them in the rough texture inside the runners. The relief valve is so small and hidden that you would not notice it even if you figured out there was a hidden chamber in the intake. We pumped it up with our compressor and at 500 it started hissing and at 50 there was the tiniest little tick sound and the hissing ended. There are no parts to it that can be seen and only one moving part.
Mr. Paul said that others would catch on and waste as much time getting ready to race to let the other guys gas run out. He called this burning them down. I looked this up and it was common to see this happen in the 70s and 80s. He said once it was figured out everyone who did this had to come up with something different.
With instructions from Mr. Paul we are replacing the rods and pistons with arias set ups 2 ford and 6 chyslers and will drop the compression to 12 to 1 and we are swapping out the distributor with a new msd. The tunnel ram had tops for 2 kindig box carbs. These were early preditor style carbs so we are going to try to get that set up running. He says we should have an easy 750hp without the gas and over 800 with it. We get the rods and crank back from the machine shop in a few weeks and then will get it all put back together. We are getting help from a local racer who builds 351 based racecars he thinks this is the coolest thing he has ever seen.
We are still figuring out what the car is and who may have been building it but are hitting dead ends. Once we get more details I will post pictures and are certain we own it free and clear.
I found the paperwork for motor work done from Paul Machine in Jupiter Florida from 1970 and tracked down the man who owned the shop who is known on 7173 as Paul of mo and he still had the motor so I was able to buy a vintage boss 351 prostock that was built with all of the best tricks and mods of the days. I have talked more to Mr. Paul in the last few weeks. He did not sell the engine because rules changed and Ford droped out of draagracing in 72. He said the engine was an experiment and he couldn’t sell it. Heres why.
The crank is stroked for 6 of the 8 rods. In the car the tech inspection could really only check the front 2 sparkplug holes for the stroke. The more cubic inches the motor had the bigger the weight penalties.
The distributer is a one of a kind homemade part that does not work like anyother dist and it does not have a limit to how fast it can work.
The heads have port plates and intake side stuffers with titanium valves and springs. The block is all rerouted for the oil and has lines running everywhere. It also has been set up for a vacume pump system to take the pressure out of the engine for more hp.
It has a homemade tunnel ram that was made to fake a weiand but works above 10000rpm.
New stuff,
We discovered that the bottom of the intake that covers the valley had 2 parts and was hollow inside with a passage cast into it that runs up to a intake bolt hole?? We found another port inside that had a tiny pressure valve in it but did not go anywhere?? I called Mr. Paul and this is what he told me.
1 of the intake studs was hollow and had a hole in it that lined up with the hole in the intake. You could screw a line onto the top of the bolt and pump nitrous into the manifold. The other valve could be shimmed to open at about 450 pounds. You filled the intake to about 400 pounds when the motor was cold. When the temp went up then the pressure in the chamber went up with it and once it hit 550 it would open the valve and let the gas flow threw very small wire drilled passages that runs to each intake port. It took about 2 min for the gas to go out. That would be long enough to do a burn out get set up and make a pass before there was no more gas left. The holes are so tiny that you can not even see them in the rough texture inside the runners. The relief valve is so small and hidden that you would not notice it even if you figured out there was a hidden chamber in the intake. We pumped it up with our compressor and at 500 it started hissing and at 50 there was the tiniest little tick sound and the hissing ended. There are no parts to it that can be seen and only one moving part.
Mr. Paul said that others would catch on and waste as much time getting ready to race to let the other guys gas run out. He called this burning them down. I looked this up and it was common to see this happen in the 70s and 80s. He said once it was figured out everyone who did this had to come up with something different.
With instructions from Mr. Paul we are replacing the rods and pistons with arias set ups 2 ford and 6 chyslers and will drop the compression to 12 to 1 and we are swapping out the distributor with a new msd. The tunnel ram had tops for 2 kindig box carbs. These were early preditor style carbs so we are going to try to get that set up running. He says we should have an easy 750hp without the gas and over 800 with it. We get the rods and crank back from the machine shop in a few weeks and then will get it all put back together. We are getting help from a local racer who builds 351 based racecars he thinks this is the coolest thing he has ever seen.
We are still figuring out what the car is and who may have been building it but are hitting dead ends. Once we get more details I will post pictures and are certain we own it free and clear.