- Joined
- Nov 15, 2016
- Messages
- 652
- Reaction score
- 15
- Location
- Australia
- My Car
- 1972 Mustang Coupe 302 Auto RHD
G'day everyone
I have been away for a while enjoying driving my 72 coupe even entered a few car shows with plenty of interest in the only 7173 in attendance
As some of you may remember I had some issues with my stroker engine last year in which it prematurely retired due to thrust failure along with (perhaps?) tight bearing clearances contributing to a sudden loss of oil pressure
Engine machinist couldn't find anything conclusive and just put it down to tight bearing clearances
My memory not being the best I believe I had checked them against the tolerances listed in my performance rebuild book which at about .0010 to .0015 I can vaguely remember the flexi-gauge reading was about .0015 which would be fine for a stock engine but have since learnt a bit tight for a performance engine
Kicked myself up the backside severely for this and decided to pay the experts to assemble the short block this time round - almost $5K for this one
Last Sunday went for a run and started to notice an odd rubbing/rattling sound coming from the engine/trans area
Oil & temp still good so took it easy and got it home to inspect
Sound was coming from the bellhousing area so suspecting a loose/cracked flexplate I removed the inspection plate
After looking for anything obvious I decided to lever on the flexplate and sure enough it moved about 3/16 inch so was hoping just a flexplate but after talking to my trans guy who knows the car well he said he wanted to look at it as it could be the engine thrust again and my first thought was no not again!
Sure enough once on the hoist with one watching the balancer and one levering on the flexplate they both moved in unison - damn damn damn!!!!
Now before anyone chimes in we previously explored the trans/convertor excess pressure on the crank causing thrust failure but didn't find anything conclusive but despite this replaced the converter and had the trans guy go over the transmission regardless
Although the engine has been going well the last few months it has recently been using a tiny bit of oil with a couple of times at high rpm (limited 5900) there has been a little smoke and not just from the tires so my gut feeling was something wasn't right
Naturally I'm devastated that once again I have to tear down the engine but first I need to conclusively eliminate the transmission side of things so will be doing a pressure test today, My trans guy who has worked on and driven this car several times has doubts the trans/converter is doing this because if the line pressure was excessive I should have extremely hard shifts which is certainly not the case
I'm also going to check every other avenue including trans alignment and crank run out as the block was align honed
The only other thing that could be causing premature thrust failure is it is just a bad crankshaft from the start
Crank is a Scat 9000 series cast and these are supposed to be good to 600hp
I have not found many negative reviews of this crank but who knows?
Anyway a long way to go and can't afford to let this happen again so will be a long process to find the cause
I will welcome any suggestions from members but reckon by now I have researched every possibility ten times over
Can't afford to fix it straight away anyway, apparently there's some bug getting around and the missus has had to close her business down so no extra cash for the mustang unfortunately
Reckon the crank is beyond repair this time so will probably go with a forged 4340 this time round. Also the block may be buggered as well but have a spare standard bore block so hopefully the pistons/rods are still good.
I have been away for a while enjoying driving my 72 coupe even entered a few car shows with plenty of interest in the only 7173 in attendance
As some of you may remember I had some issues with my stroker engine last year in which it prematurely retired due to thrust failure along with (perhaps?) tight bearing clearances contributing to a sudden loss of oil pressure
Engine machinist couldn't find anything conclusive and just put it down to tight bearing clearances
My memory not being the best I believe I had checked them against the tolerances listed in my performance rebuild book which at about .0010 to .0015 I can vaguely remember the flexi-gauge reading was about .0015 which would be fine for a stock engine but have since learnt a bit tight for a performance engine
Kicked myself up the backside severely for this and decided to pay the experts to assemble the short block this time round - almost $5K for this one
Last Sunday went for a run and started to notice an odd rubbing/rattling sound coming from the engine/trans area
Oil & temp still good so took it easy and got it home to inspect
Sound was coming from the bellhousing area so suspecting a loose/cracked flexplate I removed the inspection plate
After looking for anything obvious I decided to lever on the flexplate and sure enough it moved about 3/16 inch so was hoping just a flexplate but after talking to my trans guy who knows the car well he said he wanted to look at it as it could be the engine thrust again and my first thought was no not again!
Sure enough once on the hoist with one watching the balancer and one levering on the flexplate they both moved in unison - damn damn damn!!!!
Now before anyone chimes in we previously explored the trans/convertor excess pressure on the crank causing thrust failure but didn't find anything conclusive but despite this replaced the converter and had the trans guy go over the transmission regardless
Although the engine has been going well the last few months it has recently been using a tiny bit of oil with a couple of times at high rpm (limited 5900) there has been a little smoke and not just from the tires so my gut feeling was something wasn't right
Naturally I'm devastated that once again I have to tear down the engine but first I need to conclusively eliminate the transmission side of things so will be doing a pressure test today, My trans guy who has worked on and driven this car several times has doubts the trans/converter is doing this because if the line pressure was excessive I should have extremely hard shifts which is certainly not the case
I'm also going to check every other avenue including trans alignment and crank run out as the block was align honed
The only other thing that could be causing premature thrust failure is it is just a bad crankshaft from the start
Crank is a Scat 9000 series cast and these are supposed to be good to 600hp
I have not found many negative reviews of this crank but who knows?
Anyway a long way to go and can't afford to let this happen again so will be a long process to find the cause
I will welcome any suggestions from members but reckon by now I have researched every possibility ten times over
Can't afford to fix it straight away anyway, apparently there's some bug getting around and the missus has had to close her business down so no extra cash for the mustang unfortunately
Reckon the crank is beyond repair this time so will probably go with a forged 4340 this time round. Also the block may be buggered as well but have a spare standard bore block so hopefully the pistons/rods are still good.